Shook down the rear axle install at Hawk Pride on 12/17/22. See the Hawk Pride write up in the Wheeling Trips section.
Hawk Pride Trip
Axle itself-
The Rear Axle seemed to work great, I was a little worried about the locker since I bought a used axle but the locker seemed to work, the Ford Explorer breaks that I installed seemed to work, the parking brakes worked, etc.... I seemed to have good clearance with the RJ60 and my LCA brackets seemed to give me a little more clearance.
Control Arms and Suspension-
Overall I was very happy with the suspension. When I loaded up all my gear the day before the shocks did not compress as much as I thought they would so at normal ride height I had approx 6.5" up and 5.5" down. But I set it up with the spring just coming loose at the lowest so I should be getting as much down as needed. I also was concerned about not having a rear sway bar, but I didn't even really notice a difference without it.
I beat it pretty hard in the rocks and all my welds seemed to hold up. I also kicked it up into 2H on a few of the access roads and opened her up to let the rear suspension work and it seemed to work great, I never really opened it up on bumpy access roads with the short arms installed so I really have nothing to compare it to but I was happy with it.
I was worried about hitting the control arms in the rocks since the mounts are further fwd and outside of the "tire", but it was really a non-issue.
I still have some wheel hop (bouncing) so my antisquat must still be pretty high. I really don't want to lower the lower axle side brackets anymore due to clearance. I have a little room to go up on the upper frame side brackets but that will be a ton of work to accomplish, so I think I am going to wheel it a few more times to see how it does in different conditions and in different rocks (Windrock, Hot Springs, Green Acres, etc...) then I will make my decision.
Exhaust-
I was worried about the exhaust being too loud, but I actually liked the way it sounded
Issues not related to Rear Axle:
My front locker did not work from the very start of the trip. Need to troubleshoot.
Sliced the sidewall on Mickey Thompson MTZ tire. I think I put three plugs in it and it is holding for now.